Pardon no update. Back wrenching this week and should report back after backing-off spring adjuster soon.
Re last reply: "gas", "plugs, wires"???
The only possible commonality with this Cummins thread would be trans and I had mine pro rebuilt with a HD Goerends torque converter. Sorry, no help...
Update:
Arrived to pick-up truck: NO change!
Likely just a language barrier issue with Obi-Juan-Kinobe; good guy, and I trust his diesel skills.
The bov port on the exh man is already bolt-plugged. It seems likely that the valve is stuck partially-closed, restricting exhaust flow. I have no...
Problem solved & solution confirmed:
- 70% Exhaust manifold gasket leak,
- 30% Trans internals or Torque Converter.
[Actually, given that I had the trans/TC work done BEFORE the man gasket, I can't be certain that the gasket wasn't the entire problem. More a 'gut-sense' of reduced shudder when...
Thanks for the speedy reply!
I think the cummins tech mentioned a potential boost-pressure issue during test-drive. My Espanol is so-so, but "presione del turbo, e sistema de metra por controllo" etc.
Re motor mounts: Maybe, but given the abrupt and specific rpm window of the shaking? I'd...
1st post: all respect to the grey and grizzly!
My first Cummins. Wrenched on many of my prior Ford 6.9/7.3 idi's, P-strokes, etc. Minor Soob expert.
Just bought a '97 2500 4x4, 47re, ext. cab. 350k miles. Price was low due to a very particular shaking problem.
Conditions:
Only between...
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